Fujitsu Hot Chip Racing
 
2003 Open Track Challenge

Day Three - Buttonwillow Raceway Park (Buttonwillow, CA)

"Seven at 7s"

After a long day and an even longer drive, we were up early and at the track by 6:45am to unload the car and drive it over to 7s Only Racing for suspension work.  Tom takes the car right in and Eric sets about checking the current condition of the suspension before he starts working on things.  It's a good thing we made an appointment because three other teams show up at the same time.

Eric starts working on the car and the problems come one after the other.  The suspension setting are way out of line.  The right and left are different and there is more than an inch of toe out.  The front and back don't even come close to lining up.  The car was incorrectly setup for oval racing when it was delivered from Pro Fabrication and our previous efforts to fix this were obviously unsuccessful.  Eric comments on how difficult the suspension is to adjust and we can only agree.  While checking the car, Eric notices that many of the heim joints are either loose or binding.  They're all very cheap parts and they'll need to be replaced.  We also discover that the rear is toed out 1/16" on one side meaning the rear axle is bent.  To add insult to injury, both rear axle seals are leaking copious amounts of gear oil.  Aligning the car takes five hours and a lot of cursing so we miss both morning sessions.

We found out on the radio that a U2 NSX had hit the pit wall after going off and trying to save it on Sunrise (the last turn onto the straight).  The back of the car was all torn up and they brought it by 7s Only to see if there was anything they could do.  It looks like the engine was spared but there seems to be something broken in the left rear suspension.  Ouch.  Someone has either hit that wall or come very close every time we've run Buttonwillow counterclockwise.

Eric next put the car on the scales to be corner balanced and we got even more bad news.  The cross and side to side weights were so far off we had to check the numbers twice to believe it.  It took another two hours of work and 100 pounds of ballast in the passenger side footwell to bring the weights in line.

While all this work was going on, we discovered that our starter never showed up at the track office.  It turns out that FedEx routed the shipment to the wrong center and couldn't get it anywhere for two more days.  So much for the "World on Time".  I'd checked in with the shop earlier in the day and they located a used starter for around $100 from a place in town.  They had picked it up and were going to FedEx (here we go again) it to Thunderhill for delivery tomorrow.  I told FedEx to reroute the original shipment to Thunderhill as well, but we wouldn't get it until the next day.

After seven hours in the shop (and $809), the car was ready for the track.  Since I knew Dave would be faster than me and we would only get one shot for the day, I gave up my slot and we got him push started and on his way to pre-grid.  I settled up with Eric and Tom, who did an awesome job on the car, and headed over to our trailer to start cleaning up and organizing so we could get the car loaded as soon as the session was finished.  Dave went out and ran a 2:21.684 which isn't bad at all for his first session, not to mention the fact that the car felt totally different than the day before with the new suspension setup.

After his run, we shut down the car and finished cleaning up the trailer.  When we were ready, we tried to push start the car without success.  After a few tries, we noticed that the fuel pressure was low to zero and the pump sounded funny.  When it rains, it pours!  We unhooked the truck from the trailer, got out the tow strap and towed the car back over to 7s Only.  Eric checked the filter and all the lines but there didn't seem to be anything blocked.  He put it all back together and the car started right up.  Eric thinks we might have uncovered the fuel pickup and sucked a bubble into the lines.  Eric and Tom refused to take any more of our money for this quick fix and told us to get lost before we broke something else!  We headed back to the trailer, loaded the car and hit the road.  We were the last group out of the track and plenty tired with a 400 mile plus drive to Thunder Hill ahead of us.

After driving for a few hours, we stopped for gas and food and a driver change.  I decided to take a look around our rig before we left and discovered that one of the trailer tires was flat.  We put air in and it didn't seem to have a fast leak so we decided to press on and check it every so often.  We stopped about an hour later and it was only down ten pounds so we changed drivers and kept rolling.  Dave wasn't feeling well so I ended up driving most of the way with one more stop for fuel.  We rolled into Willows on the heels of a Touring RX-7 sometime after midnight and went straight to bed.

 

                          

               

            

 

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